coldiniowa
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IF you have checked all the negative & positive connections - at both ends! And if the problem is persisting, there are a few things to keep in mind. The first is thermal expansion & the second is polyester resin. Why? Because When things warm up they expand but contract when cooled off. You could have a bad ignition coil but it may bench test fine (when it's cool) but still have a hairline crack in the middle of the thing where you cant see it, but after it is mounted on the engine & it comes up to normal temp, the crack can expand, causing a break in the internal coil wire winding - which is encased in polyester resin. The same problem can affect a crank, cam or knock sensor as well.
Now - IF it runs fine when cool, then peters out after warming up & starts up rough or not at all, as if it ACTS over heated when it is not, the issues is typically the EGR valve. The later model EGR units are solenoid controlled & the coil winding for those are also likely to be encased in resin & may have a crack you cant see then may also be affected by the same issue I mentioned above. In older units that have vacuum controlled EGR's, there is a carbon build up that caused the internal piston of the unit to get stuck. For that issue, you need to remove it, hit it a few good times with penetrating oil, then smack the protruding rod against a hard surface CAREFULLY & straight a few times, then blow it out with compressed air & repeat these steps a few times if needed, then re-install with a new gasket.
I hope this helps.
Now - IF it runs fine when cool, then peters out after warming up & starts up rough or not at all, as if it ACTS over heated when it is not, the issues is typically the EGR valve. The later model EGR units are solenoid controlled & the coil winding for those are also likely to be encased in resin & may have a crack you cant see then may also be affected by the same issue I mentioned above. In older units that have vacuum controlled EGR's, there is a carbon build up that caused the internal piston of the unit to get stuck. For that issue, you need to remove it, hit it a few good times with penetrating oil, then smack the protruding rod against a hard surface CAREFULLY & straight a few times, then blow it out with compressed air & repeat these steps a few times if needed, then re-install with a new gasket.
I hope this helps.